Faculty Of Engineering Graduation Project 2023 - 2024
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Browsing Faculty Of Engineering Graduation Project 2023 - 2024 by Subject "October University For Modern Sciences and Arts"
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Item Reducing Cycle Time in Nivea Deodorant Production Line(October university for modern sciences and arts, 2024) Ayman Saleh, Karim; Adly Hamed, NermeenScitra Contract Production factory has been specializing in personal and home care in UAE since 1976. Since 2016, the Egyptian branch has been located in the industrial zone in 6th October City. Furthermore, the plant has swiftly gained a reputation as one of the finest quality producers, which assists other companies in raising their productivity. Scitra specializes in personal care and home care products from firms such as Nivea, Rexona, Tide, Dove and Vanish. After investigating the whole production process of Nivea Deodorant product, it was found out that the washing process of the mixers used to take four and a half hours to be washed, rinsed and sterilized. Furthermore, the pre-weighing process takes around two hours to prepare and weigh all the needed materials to be mixed. Additionally, the changeover time is a considerable delay resulting in a full stoppage for the whole production line for five hours long to change from a size to another. Finally, there is a frequent stoppage occurred in Nivea Deodorant production line because of lack of knowledge of the workers in operating the Cap Screwing machine. The project aims to reduce the time waste of the aforementioned problems which will reduce the cycle time of Nivea Deodorant production process, and the results obtained demonstrated a 15% reduction in cycle time. This is achieved by using industrial engineering techniques such as Operation Analysis, DMAIC, 5S, Value Stream Mapping (VSM), Correlation and Regression Analysis, and Single Minute Exchange of Dies (SMED).Item Waste Reduction in a Cooker’s Glass Processing Factory(October university for modern sciences and arts, 2024) Magdy Mohammed Hassan, MohammedUnion air Cooker’s Glass Processing Factory is specialized in manufacturing of different glass products such as cookers, ovens, televisions, heaters, fridges, and deep freezers glass faces. It is a part of Union air Group, which has been operational since 1995, and is recognized for its innovative and high-quality products such as air conditioners, washing machines, refrigerators, and cookers. The glass factory is located in Industrial zone, 6th of October, Giza, Egypt, the factory was established in 2017. The factory produces annually 768,000 square meters of glass products. The aim of this project is to identify the wasted glass material in all glass processing stations and analyze this data to propose suitable solution in order to minimize waste and improve productivity in the factory. The initial status of the factory is that it is highly inefficient and suffering huge losses that have not been reliably quantified prior to this project. This project focuses on implementing lean production techniques such as 5S, standard operation, maintenance routine checklist, employee training, and quality control to reduce the wasted material. The achieved result showed that the glass waste is reduced from 30% to 15%, with total saving per year of approximately 9 Million LE.Item Waste Reduction in a Corrugated Cardboard Factory(October university for modern sciences and arts MSA, 2024) Mohsen, Saif TarekUniversal Unipack has two branches specialized in packaging industry. It manufactures corrugated cardboard and prints on it. It was established in 1981, at the second industrial zone at 10th of Ramadan city-Egypt, the other branch is located in the Sadat city. After investigating the corrugated cardboard production line, it was found that there are two main problems in the factory. First, there are a lot of scrap that comes out from the production line, the average for production in a month is 2495.2 tons which has 290 tons waste from the production process which is about 12%. Secondly, the layers of cardboard peel off easily because of bad starch that they use to glue the layers with each other. This project aims to reduce waste in a corrugated cardboard factory from 290 (tons per month), which will reduce the material waste by almost 14 % and save them 920,000 L.E by using lean six sigma and 5s methodology. The achieved results will be increase the productivity of the corrugated cardboard by reducing the waste in the production line.